Hi,
Sorry to hear that but we still didnt pull this ESP due to priorities... you know.
I will share the findings once we pull it and dismantle it.
Thanks,
Good Day,
We always use the Echo-meter for the fluid shot which will be taken inside the casing to measure the fluid level and calculate the down hole intake pressures.
Was echo-meter been used before in the well head to detect the tubing holes by the acoustic graph?
And how can it detect the...
Many thanks for the tips. Unfortunately the ESP failed before carrying out a production testing to know whats going on exactly.
It will be scheduled for dismantle job when its pulled out.
Thank you all for your support.
Hello,
Well, the ESP was installed in a high gas well.
Pi is the pressure obtained by the sensor for the ESP pump intake pressure and Pd is the discharge pressure at the pump discharge.
so Pi supposed to be at the bottom and Pd is at the top of ESP inside the tubing.
Regarding the flowrate, its...
Hello,
yes its running of VSD and after the trip Pi was stabilizing at 934 psi and Pd dropped down to 518 psi which makes me surprised.
There is already check valves but on the surface flowline not on the D/H production tubing. the Pd dropped lower than Pi within 12 minutes only.
Many Thanks...
Hi Everyone,
I have a case with an ESP where its tripping due to U/L. But after the ESP trip, Pd dropped less than Pi.
Can you please inform about this situation?
Note: ESP is installed in High gas well.
Many Thanks,