alexander123097
Electrical
- Apr 26, 2014
- 5
This application is on a roll grinder. The motor is turning a grinding wheel using v belts from motor to grinding wheel spindle. 40hp DC mill duty motor mounted horizontal on a carriage, the carriage traverses back and forth. The motor is driven by a digital drive using an analog tach feedback. The motor has sleeve bears (babbit), do not the spec. on end play (axial movement of the shaft). I work in an electrical maintenance & control department at a steel mill, the grinder mentioned is a roll grinder
First called on problem because it had threw belts, told motor had not been installed that long ago. Do not know exactly why the replacement was needed or how long it was in operation. Belts were replaced and monitored operation and motor was surging or thrusting, the shaft would slide back and forth almost a quarter inch. Operations and machine maintenance said there has always been end play but nothing like this. The tach assembly had a love-joy coupling and it was not mounted correctly. Set the drive up to run from tach feedback to voltage feedback and tuned to compensate, operation looked ok & operated for a few days. A new tach arrived with proper machined shaft and a different coupling, it is a collapsible type. Did not stay close to problem but Area wanted these parts installed and switched back to tach control, it had been operating that way for years without issues. Later, about 4 days, the motor started surging or thrusting, the shaft would slide back and forth almost a quarter inch. There was darkness in the bearing oiler so the decision was made to change motor because of the bearing, although it did not feel hot. A new motor, repaired at the same machine shop that has done all these motors, was already onsite so decision was made to replace. This motor had been ran for hours offsite by the motor supplier with no load only putting voltage on the buss and letting it running giving it a pass fail test, it passed. This motor was installed but unable to put in operation. It looked ok when first installed but after running an hour it started surging or thrusting, the shaft would slide back and forth almost a quarter inch. Removed the belts (removing load) & connected an analyzer up and monitor. Motor would act normal at low speeds but when turned up to high RPM it would thrust. Also it would thrust when the carriage that it sets on moves at either RPMs. Adjusted the field as high as possible (probably could not operate at this setting and problem remained). Did not see motor current on analyzer surge, it looked steady. Had an alignment group check the motor level, it was good. Had a GE Drives person come in but he could not find issue with drive. He is not an application grinders person only works on drives on many different types of systems. We all were and are left with no more ideas. This motor never was able to be put in service. The motor supplier states and it did run ok at his shop using a DC supply. Another motor was coming back from machine shop so the decision was made to install and align getting all people together and start it up and monitor operation. Did that and the first roll it ground all looked ok. Vested people left, it ran maybe an hour total, then it started thrusting slightly( not like the motor that was removed). But is that normal or is this how the problem started?
The grinder was shut down until tomorrow so we all have a chance to think it over and get a person coming in that works on grinders. Not sure it he will have further input. Do not want to compromise the motor by continuing to run it with questions. I believe he will say replace drive but do not know. I am looking for a spare drive we may have that we can temp install just to run motor if asked. At this point will follow his thoughts because we are at a loss at our site. Our department clovesr so much area and systems do not know exact details of all equipment. How much end play on a 40hp motor that is belt driven not coupled to a gearbox, no idea.
This site has been a great resource for me. Anyone have any thoughts on this?
First called on problem because it had threw belts, told motor had not been installed that long ago. Do not know exactly why the replacement was needed or how long it was in operation. Belts were replaced and monitored operation and motor was surging or thrusting, the shaft would slide back and forth almost a quarter inch. Operations and machine maintenance said there has always been end play but nothing like this. The tach assembly had a love-joy coupling and it was not mounted correctly. Set the drive up to run from tach feedback to voltage feedback and tuned to compensate, operation looked ok & operated for a few days. A new tach arrived with proper machined shaft and a different coupling, it is a collapsible type. Did not stay close to problem but Area wanted these parts installed and switched back to tach control, it had been operating that way for years without issues. Later, about 4 days, the motor started surging or thrusting, the shaft would slide back and forth almost a quarter inch. There was darkness in the bearing oiler so the decision was made to change motor because of the bearing, although it did not feel hot. A new motor, repaired at the same machine shop that has done all these motors, was already onsite so decision was made to replace. This motor had been ran for hours offsite by the motor supplier with no load only putting voltage on the buss and letting it running giving it a pass fail test, it passed. This motor was installed but unable to put in operation. It looked ok when first installed but after running an hour it started surging or thrusting, the shaft would slide back and forth almost a quarter inch. Removed the belts (removing load) & connected an analyzer up and monitor. Motor would act normal at low speeds but when turned up to high RPM it would thrust. Also it would thrust when the carriage that it sets on moves at either RPMs. Adjusted the field as high as possible (probably could not operate at this setting and problem remained). Did not see motor current on analyzer surge, it looked steady. Had an alignment group check the motor level, it was good. Had a GE Drives person come in but he could not find issue with drive. He is not an application grinders person only works on drives on many different types of systems. We all were and are left with no more ideas. This motor never was able to be put in service. The motor supplier states and it did run ok at his shop using a DC supply. Another motor was coming back from machine shop so the decision was made to install and align getting all people together and start it up and monitor operation. Did that and the first roll it ground all looked ok. Vested people left, it ran maybe an hour total, then it started thrusting slightly( not like the motor that was removed). But is that normal or is this how the problem started?
The grinder was shut down until tomorrow so we all have a chance to think it over and get a person coming in that works on grinders. Not sure it he will have further input. Do not want to compromise the motor by continuing to run it with questions. I believe he will say replace drive but do not know. I am looking for a spare drive we may have that we can temp install just to run motor if asked. At this point will follow his thoughts because we are at a loss at our site. Our department clovesr so much area and systems do not know exact details of all equipment. How much end play on a 40hp motor that is belt driven not coupled to a gearbox, no idea.
This site has been a great resource for me. Anyone have any thoughts on this?