Guest
We had a contractor pour a six inch slab 80 x 100' over two new underground storage tanks with 14' of 3/8" clean aggregate backfill, drop poured into excavation after aggressive hand compaction of aggregate under and around tanks. No mechanical compaction of subgrade was performed until final 10-12". Walk behind plate tamper was used by contractor and site was leveled.
Contractor told me that instead of highway mat, hex mesh or conventional rebar he would recommend fibermesh concrete with a 5000# PSI only; no reinforcement was needed. He fine graded the site with approximately 1"+/- CA6 over the CA16 without filter fabric separation. Traffic, including our delivery of gasoline (Tanker carrying approx. 7K gal.) was allowed over pavement in 4 days...avg. temp. 45 degrees F.
Within 7-10 days cracking started. I need help.
1. What specifications should he have used, or me?
2. Was he correct that the fibermesh in concrete mix was sufficiently strong enough for the depth of backfill shrinkage from traffic vibration?
3. No engineer was used to specify concrete, etc.
4. At 96 density proctor the 4% loss by self compaction of the subgrade; according to the contractor, could result in a 5.5 inch loss under the concrete?
5. It would help me convince the contractor to repair his problem if I had some references from knowledgeable sources or ASTM/ANSI/ACI, etc. I have spent an inordinate amount of time trying to research this without a MAP!
Thanks.
Contractor told me that instead of highway mat, hex mesh or conventional rebar he would recommend fibermesh concrete with a 5000# PSI only; no reinforcement was needed. He fine graded the site with approximately 1"+/- CA6 over the CA16 without filter fabric separation. Traffic, including our delivery of gasoline (Tanker carrying approx. 7K gal.) was allowed over pavement in 4 days...avg. temp. 45 degrees F.
Within 7-10 days cracking started. I need help.
1. What specifications should he have used, or me?
2. Was he correct that the fibermesh in concrete mix was sufficiently strong enough for the depth of backfill shrinkage from traffic vibration?
3. No engineer was used to specify concrete, etc.
4. At 96 density proctor the 4% loss by self compaction of the subgrade; according to the contractor, could result in a 5.5 inch loss under the concrete?
5. It would help me convince the contractor to repair his problem if I had some references from knowledgeable sources or ASTM/ANSI/ACI, etc. I have spent an inordinate amount of time trying to research this without a MAP!
Thanks.