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  1. rota1

    Sundyne Model LMV-341

    Hello Johnny Pellin Some suggestions 1)check the depth of the recess in the impeller that meets the shaft shoulder,if the recess is not deep enough, torquing the locknut would not give adequate compression on the O rings/sleeve/rotary seal to achieve the required friction to prevent spinning...
  2. rota1

    Ruhr Pumpen pumps

    Thanks very much for the information.Basically what you guys are saying is their pumps are reliable, we would have to be concerned with back up service.
  3. rota1

    Repeated Disaster Bushing Failure

    Again thanks to everyone for commenting. Mike Halloran :The component that I am referring to (Disaster bushing) is also referred to as the throttle bushing. No we didn't figure out what went wrong in the first place, these two failures took place within seconds in one instance, and about a...
  4. rota1

    Repeated Disaster Bushing Failure

    Thanks Mike ! for the quick response, but could you elaborate some more! Concentricity and perpendicularity checks was carrried out during the overhaul and was found to be 0.003 thou.
  5. rota1

    Repeated Disaster Bushing Failure

    Hello everyone We have a between bearings Union centrifugal pump in a high temperature (700deg F) high viscosity service.After shop overhaul the disaster bushing failed during startup.The bushing was fused against the seal sleeve.This disaster bush is made of bronze and has a diametral...
  6. rota1

    Ruhr Pumpen pumps

    Hello all, Does anyone have experience with Ruhr Pumpen pumps particularly in hot hydrocarbon service?.Thanks
  7. rota1

    OB thrust bearings discolouring oil

    Hello guys! Thanks for all the invaluable information.This is a follow up question, we have verified the thrust bearing on this pump is skf 7409 BCBM and discolouring oil, the OEM says it should be skf 7409 BG, we have now changed to this and the discolouring has stopped.Our research says that...
  8. rota1

    OB thrust bearings discolouring oil

    Thanks guys! How will we know that we have assembled the bearing correctly? is there a procedure? I have never seen one! if there is, one can you guys supply me with it! Thanks again guys!
  9. rota1

    OB thrust bearings discolouring oil

    Hello all! we have here a Byron Jackson two stage, between bearings, boiler feed water pump that discolours the oil upon minutes of being put in service,bearings are skf 7409BG, and the driver is a motor running on a magnetic center.Coupling is a Waldron gear type, the spool piece has axial...
  10. rota1

    Sundyne pump model LMV 311

    Thanks JJPellin A test done on one of the pumps running solo revealed a discharge head of 2200 head ft and a flow of 76 gpm (running below the rated point) The pump is designed to run at discharge press of 2748.0 head ft (899.8 psig) and rated flow of 88 US GPM pumping propane (SG 0.5)...
  11. rota1

    Sundyne pump model LMV 311

    Thanks guys for the excellent information.We have a similiar problem whereby there are four pumps running in parallel.Even so, designed head and flow cannot be achieved, we have found that the diffuser discharge exit port is 10 thou larger than what it is supposed to be, contractor is telling...
  12. rota1

    Sundyne pump model LMV 311

    Hi guys! Can you guys explain to me what in the design of this pump is so unique that allows for the high head and flow developed ? some one mentioned it is all in the discharge diffuser exit port?
  13. rota1

    Reducing Impeller Diameter

    Hi Guys! I have to reduce an impeller diameter. Should I cut both vanes and shroud or only the vanes. My thinking is only the vanes are to be reduced, maintaining impeller to cut water original clearance (Gap B).A strange school of thought has surfaced viz; that reducing the shroud eliminates...
  14. rota1

    single sealed vs shield ball bearings

    Thanks a lot Electricpete, and what about if its either a single or double seal or shield? I was thinking that it was the number of points of sealing that determined if it was a single or double.
  15. rota1

    single sealed vs shield ball bearings

    Hello everyone, This may seem as too basic a question but nevertheless, I am having a problem in understanding what is the difference if any, between a SEAL as opposed to a SHIELD bearing.
  16. rota1

    Motor Running above Overload point

    Thank you Waross..... in the shut off mode,from the pump curve, we see the power required is 50HP..with this new information can you say the shut in current of 17Amps is ok for this motor.
  17. rota1

    Motor Running above Overload point

    Thanks a lot guys for such valuable input. I forgot to mention that during our shut off head test(motor on no load) the ammeter reading was 17Amps, is this indicative of some problem? it seems to me that there is a little difference of Amps between no load and load(24.3A) This motor is 100 HP...
  18. rota1

    Motor Running above Overload point

    Thank you Alexit....some additional information... On our shut off head test we measured the rpm of the motor,this equalled to 3581 rpm, on opening the control valves we observed the motor speed to be 3561 rpm, bear in mind that the rated speed on the nameplate is 3565rpm. What we know is the...
  19. rota1

    Motor Running above Overload point

    Thanks CCOR for the quick response, the motor rotation was checked and verified to be correct.
  20. rota1

    Motor Running above Overload point

    Friends, Please advise! We have here a two stage centrifugal pump, 157gpm capacity, at 995 ft head.This pump is in a water injection service supplying three streams, the flow is controlled via valves which are throttled to meet requirement. The motor driver is 100HP.According to the pump curve...
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