GasOilEng
Petroleum
- Mar 3, 2017
- 23
Hi everyboy
I am process engineer in LPG plant. The oily water generated from regeneration phase of MolSiev bed of natural gas is sent from regeneration drum working @ 90bar & 50 to 60°C to API oily water treatement unit (Working pressure 1bar, ambient temp) passing by control valve through 2" SCH40 line.
To be noted that the control valve working from 90bar to 1bar is not 100% seal when it is shut @ 100% (There is always leak, formation of ice on outer surface of this line).
What happened is that the deformation of the latter line, see attached photo, has been occured.
Is any one has an explaination of this phenomenon.
If yes, Is it correct if we change the diameter from 2" to 3 or 4".
Thanks for your helps.
Best Regards
I am process engineer in LPG plant. The oily water generated from regeneration phase of MolSiev bed of natural gas is sent from regeneration drum working @ 90bar & 50 to 60°C to API oily water treatement unit (Working pressure 1bar, ambient temp) passing by control valve through 2" SCH40 line.
To be noted that the control valve working from 90bar to 1bar is not 100% seal when it is shut @ 100% (There is always leak, formation of ice on outer surface of this line).
What happened is that the deformation of the latter line, see attached photo, has been occured.
Is any one has an explaination of this phenomenon.
If yes, Is it correct if we change the diameter from 2" to 3 or 4".
Thanks for your helps.
Best Regards