hacksaw
Mechanical
- Dec 7, 2002
- 2,564
A historical thermowell failure was reported during process warmup (condensate)
Pressure 2500 psig
Temperature 100 Deg F initially 650 at normal conditions
NPS 16 SCH 160 with flows in the 10000 gpm range
Pipe Mtd Well Dimensions 6.5"Length x 0.875"OD x 0.546"ID
Both 19.3 and 19.3TW claim the well is safe even though the well was field fabricated, but it failed in less than 100 hrs during warmup.
A tapered drilled bar stock in a adjacent part of the process was showing signs of failure risk, but did not fail at the time. All wells were later replaced or removed. The replacement designs were shorter.
quite the puzzle, comments or explanations welcome
Pressure 2500 psig
Temperature 100 Deg F initially 650 at normal conditions
NPS 16 SCH 160 with flows in the 10000 gpm range
Pipe Mtd Well Dimensions 6.5"Length x 0.875"OD x 0.546"ID
Both 19.3 and 19.3TW claim the well is safe even though the well was field fabricated, but it failed in less than 100 hrs during warmup.
A tapered drilled bar stock in a adjacent part of the process was showing signs of failure risk, but did not fail at the time. All wells were later replaced or removed. The replacement designs were shorter.
quite the puzzle, comments or explanations welcome