shyamshins
Mechanical
- May 4, 2012
- 53
Dear Sir,
I have ammonia seal leakage issue in fertiliser plant. Pump on which seal is installed is a Ammonia booster pump.
This is double seal with seal face combination of SIC V/S SIC in Inboard side & SIC V/S Carbon at outboard side.This seal has common gland which incorporates both Inboard & Outboard stationary face of SIC. Stationary & Rotary O rings are of EPT.
OBSERVATION OF FAILED SEAL :
Inboard failure observation:
Stationary SIC face found cracked in pieces & rotary SIC face cracked in pieces.
EPT O rings of both rotary & stationary face shape changed to sqaure.
Stationary SIC face has deep groove mark on its contact face.
Outboard failure observation :
Stationary SIC face has deep groove marks on its contact surface which indicates insufficient lubrication & rise in tempreture, but barrier fluid is provided for lubrication.O/B rotary carbon face is found scored.
Rotary & stationary O rings shape changed to square shape.
Process Details are as below :
Process Liquid : Ammonia
Suction pressure : 17 Kg/cm2
Discharge pressure : 20 Kg/cm2
Process Temp.: 15 to 35 Deg.celcius.
Runout of pump : 0.02mm
Axial / Radial play : 0.01mm / 0.1mm
These pumps have 3mm hole at 12 O clock position for venting in stuffing box.
1.Flushing plan 11 & 53.
2.Tempreture at gland plate connection at barrier inlet to seal is 45Deg celcius & temp. at Barrier outlet from seal to thermosyphon pot is 47.6 Deg celcius.
3.Temp. at thermosyphon pot cooling coils inlet temp.( From seal oulet ) is 39.5Deg.celcius & temp. at thermosyphon pot cooling coil outlet ( towards inlet of seal ) is 40.4 deg.celcius.
4. Vapour pressure of Ammonia at 100deg. farenhite is 200 Psig.
5. Vapour pressure of Methanol (Barrier Fluid) is 100 mm of Hg / 0.133bar @ 21.2 Deg.celcius
6. Viscosity of Methanol at 100 F = 0.5 Mpas
7. Viscosity of Ammonia at 100 F = 0.01044 Cp
Pls. provide solution as this seal is failing every 4 months due to which we are not getting seal life.
I have ammonia seal leakage issue in fertiliser plant. Pump on which seal is installed is a Ammonia booster pump.
This is double seal with seal face combination of SIC V/S SIC in Inboard side & SIC V/S Carbon at outboard side.This seal has common gland which incorporates both Inboard & Outboard stationary face of SIC. Stationary & Rotary O rings are of EPT.
OBSERVATION OF FAILED SEAL :
Inboard failure observation:
Stationary SIC face found cracked in pieces & rotary SIC face cracked in pieces.
EPT O rings of both rotary & stationary face shape changed to sqaure.
Stationary SIC face has deep groove mark on its contact face.
Outboard failure observation :
Stationary SIC face has deep groove marks on its contact surface which indicates insufficient lubrication & rise in tempreture, but barrier fluid is provided for lubrication.O/B rotary carbon face is found scored.
Rotary & stationary O rings shape changed to square shape.
Process Details are as below :
Process Liquid : Ammonia
Suction pressure : 17 Kg/cm2
Discharge pressure : 20 Kg/cm2
Process Temp.: 15 to 35 Deg.celcius.
Runout of pump : 0.02mm
Axial / Radial play : 0.01mm / 0.1mm
These pumps have 3mm hole at 12 O clock position for venting in stuffing box.
1.Flushing plan 11 & 53.
2.Tempreture at gland plate connection at barrier inlet to seal is 45Deg celcius & temp. at Barrier outlet from seal to thermosyphon pot is 47.6 Deg celcius.
3.Temp. at thermosyphon pot cooling coils inlet temp.( From seal oulet ) is 39.5Deg.celcius & temp. at thermosyphon pot cooling coil outlet ( towards inlet of seal ) is 40.4 deg.celcius.
4. Vapour pressure of Ammonia at 100deg. farenhite is 200 Psig.
5. Vapour pressure of Methanol (Barrier Fluid) is 100 mm of Hg / 0.133bar @ 21.2 Deg.celcius
6. Viscosity of Methanol at 100 F = 0.5 Mpas
7. Viscosity of Ammonia at 100 F = 0.01044 Cp
Pls. provide solution as this seal is failing every 4 months due to which we are not getting seal life.