PetroDDP
Petroleum
- May 10, 2011
- 38
HP steam is generated from waste heat boiler at two places in Sulfur unit of the Petroleum Refinery one at reaction furnace and another at incnerator downstream equipment.This saturated HP Steam(261 deg C-Design value) is routed to Superheater where it is superheated to 391 deg C(Design value).Design value of Saturated HP Steam pressure is from 47.5 kg/cm2g to Design value of Superheated HP Steam pressure is 43.6 kg/cm2g.Superheater is Shell and tube type where Incinerator flue gases are used to superheat steam. (Shell side :Flue gases)
The area of concern is that actual superheated HP Steam temperature remains lower than design at 365 deg C (43 kg/cm2g actual pressure) against 391 deg C design value.
There are total 03 trains parallel to each other in Sulfur units in addition to this, all the tail gases passes through common TGTU unit, TGTU offgases are equally distributed to incinerator in three trains. other two trains Superheated HP Steam temperature remains close to the design as compare to one train where above concern/problem is faced.
potential causes for performance and remedial measures are requested.
Thanks in advanced.
The area of concern is that actual superheated HP Steam temperature remains lower than design at 365 deg C (43 kg/cm2g actual pressure) against 391 deg C design value.
There are total 03 trains parallel to each other in Sulfur units in addition to this, all the tail gases passes through common TGTU unit, TGTU offgases are equally distributed to incinerator in three trains. other two trains Superheated HP Steam temperature remains close to the design as compare to one train where above concern/problem is faced.
potential causes for performance and remedial measures are requested.
Thanks in advanced.