MacMcMacmac
Aerospace
- Sep 8, 2010
- 56
thread237-507222
In reference to the above thread: The 1MW, 1780rpm wound rotor motor is experiencing excessive axial vibration after overhaul to replace D.E. bearing which failed due to a lack of lubrication.
A year on, and this issue has not been solved. The Hail Mary play was to take out .055" of soft foot and see if that was causing problems with distortion of the frame when the final bolt-down took place, even though the alignment system said everything was ok with our installation. Everyone is frustrated by now and I get the feeling the motor shop is chasing their tail on this.
I was wondering if this might be a case of multiple magnetic centers? It seems like a long shot but everything measures straight and true, air gap is consistent, new collector rings were machined and installed for the wound rotor to eliminate the porosity found on the old rings. The rotor was sent to another shop to be balanced at higher than usual RPM to ensure everything was ok. We are on the cusp of a major testing campaign and this machine is vital to achieve certain altitude test points.
There has been a theory advanced that changing out to double row ball bearings may make the arrangement more rigid, since the motor shop's engineers stated the current bearings have way more thrust capability than is necessary, but I'm skeptical at this point.
There is the second stage exhauster next to it which has the exact same motor. Management was suggesting installing that motor on the first stage to rule out any machine vibration being transferred to the motor, but I don't see the value in this since absolutely everything points to the motor being the problem, including the motor shop personnel who stated the motor shook excessively even on their testing rig.
Any input is gratefully received.
In reference to the above thread: The 1MW, 1780rpm wound rotor motor is experiencing excessive axial vibration after overhaul to replace D.E. bearing which failed due to a lack of lubrication.
A year on, and this issue has not been solved. The Hail Mary play was to take out .055" of soft foot and see if that was causing problems with distortion of the frame when the final bolt-down took place, even though the alignment system said everything was ok with our installation. Everyone is frustrated by now and I get the feeling the motor shop is chasing their tail on this.
I was wondering if this might be a case of multiple magnetic centers? It seems like a long shot but everything measures straight and true, air gap is consistent, new collector rings were machined and installed for the wound rotor to eliminate the porosity found on the old rings. The rotor was sent to another shop to be balanced at higher than usual RPM to ensure everything was ok. We are on the cusp of a major testing campaign and this machine is vital to achieve certain altitude test points.
There has been a theory advanced that changing out to double row ball bearings may make the arrangement more rigid, since the motor shop's engineers stated the current bearings have way more thrust capability than is necessary, but I'm skeptical at this point.
There is the second stage exhauster next to it which has the exact same motor. Management was suggesting installing that motor on the first stage to rule out any machine vibration being transferred to the motor, but I don't see the value in this since absolutely everything points to the motor being the problem, including the motor shop personnel who stated the motor shook excessively even on their testing rig.
Any input is gratefully received.