Hi Swern,
The problen is really interesting ! which is the compressor service make and model of machine, is it motor dtriven ?
The phenomenon explained by you is a normal feature in high pressure centrifugal compressors. When Antisurge valve opens, the down stream of ASV or in other words suction pressure rises. This pressure rise could be quite normal and not noticeable in low pressure compressors and very high in compressors having higher presure ratio.
AA) when we have compressors in a train with 2 , 3 or 4 casing configurations with a high pressure rise across suction and discharge such as 165 bar, or 100 bar, it is a practice to provide a vent valve in discharge ( upstream of ASV)which will open alongwith ASV at the same instant of trip and remains open for 3 to 10 sec and closes. This will remove the large pressure pulse in discharge line. In one of our Syn gas compresors with 3 casing design with discharge pressure of 220 bar and suction pressure of 25 bar, we could resolve by suitably controlling the opening of vent valve timing ( time it remains open after trip )increase from 3 sec to a higher valve.
BB)you can examine if the reference gas pressure tapping from the cavity you mentioned is sluggish and blocked . unable to communicate the quick changes in suction pressure to oil inlet(i.e. cavity between mechanical seal and laby seal).
I do not know in your present case what are the pressure levels and total pressure levels and service application like FCC, gas or H2 etc. It will be appropriate to know the compressor parameters to appreciate what is happening.
Pl examine the aspects suggested by me.
"bvsrtt" has worked in BHEL, India as a compressor designer for centrifugal compressors dept at Hyderabad, India . If you like u nay contact