Mohammad Ka
Chemical
- Jul 6, 2019
- 37
Hi everyone
During start up of an ethylene plant, discharge temperature of the crack gas compressor (fifth stage) was drastically increased, meanwhile very high amount noises like fast opening and closing of a valve was observed. Moreover the compressor faced with insufficient flow. In this case, opening of the antisurge valve was 100%.It should be noted that there is no FE on antisurge loop Of CGC stage 1 and no piping pockets in the suction. However, a pumping trap is installed in upstream of suction line CGC stage 1. Antisurge valve with a difuser is specified to be a low noise
Other trends could be listed as below:
1- Outlet temperature of crack gas from quench tower was increased about 4-5 deg.C.
2-Level of discharge and suction drums of the crack gas compressor (stage 4) were increased during starup.
3-Discharge temperature of 5th stage of the CG compressor was increased to 130 C.
4- Fluctuation of flow was observed in all five stages of the compressor.
5-Alongside the flow fluctuation some small fluctuinations of pressure drop was observed in caustic tower.
6- No vibration in CG compressor was detected by DCS.
The following activities to remedy have been done:
* Antisurge valve was opened and fully inspected . No failure was detected.
* All suction and discharge drums, check valves, orifices, cooling water exchangers and caustic tower in the line were inspected and no chocking or unusual thing was seen.
* About 1000kg mixed yellow oily water was observed in cooling water exchanger of 5th stage of the crack gas compressor. Antisurge valve is branched from outlet of this exchanger. The water was completely drained.
*Stage 5 of the compressor was inspected by a borescope camera and no failure was detected.
After these remediations and start the plant for the next three times, the noise, insufficient flow and increased temperature were again repeated.
I was wondering if anyone could propose a solution?