REVenezuela
Mechanical
- Oct 9, 2010
- 9
Dear colleagues,
Looking for some advice here.
I'm new to this plant and have been assigned to solve a recurrent problem on a couple of pumps which MTBF is around 3 months combined, the characteristics and operating conditions as follows:
Pump Type; API OH4 (not very fan of these particular type of pumps by the way)
Rated Flow: 260 gpm
Normal Flow (Data Sheet): 237 gpm
Actual Flow: It varies from 154 to 176 gpm ( 56 to 64 of the BEP)
BEP: 275 gpm
Diff. Head: 237 ft
Fluid Temp.: 264 *F
Fluid: Waste Water (Traces of CO2, NH3, HCN, particles / soot fines)
S.G: 0.936
Nss: 9660
Ns:487
Speed: 3600 rpm
Impeller Diam. = 8.5”
NPSHa (Data Sheet): 13 ft
NPSHa (Calculated - Suction Gauge Pressure Method): 12 ft
Min. Flow: 70 gpm
Suction Pipe: 4.5 times straight run of pipe diameters.
Inlet Velocity: < 3.5 FPS
Volute Type: Single
Materials: A351 CF3M (Impeller, Casing Cover, Volute), Ni-Resist (Wear rings)
Mechanical Seal: JC 2800 / API Plan 74 + 13 (1 1/8"shaft diam.).
Symptoms / Findings:
I’ve been quite a bit in the field checking these pumps and a “mild” cavitation like noise could be heard all the times although may becomes worse and make all the system to shake badly (similar to water hammer), this have caused in the past cracks on weldings, supports to come loose, failed bolts, etc., slight pressure fluctuations at the discharge are evident too. I have seen this happening even when a new (spare) pump installed.
Vibration could be severe at times but in my opinion this is a consequence after the radial sleeve bearing (carbon) gets worn and the wear ring rubs and get unbalanced, high speed and a massive rigid coupling make things worse.
I have had the opportunity to inspect these pumps internally a couple of times after they failed, I will let the pictures to speak for themselves. One thing that caught my attention though was the condition of the casing compared to the impeller being made of the same materials (although I’m pretty sure they are not) which tells me sometime on the run they may have been changed (I’m tracking this with the OEM). This does not explain the problem I’m describing though, does it?. Erosion-corrosion, recirculation cavitation?.
Control / Operating / Process conditions:
The system operates on level control, waste water and high particle filtrate is fed to the tower while live steam 50 PSI is injected in the mid section of the column, normal level is 50% although most of the times is at 40%. Control of particle content seems to be an issue upstream (still working with Process eng. to understand the problem). Flow meter and one of the level controllers is not working either (working with E/I to see if it’s a process related failure) so basically the control is manual. Pump was originally provided with basket strainers at the suction but they were removed most likely because of previous failures were attributed to cavitation, a filtration system was installed downstream of the pumps instead. This filtration system operates with a battery of 3 filters in parallel and three other filters in standby, the control is completely manual, a crew of operators monitor the dP across the filters and switch to the standby filters (which is kept pressurized) when the differential pressure reach the alarm values. The mesh of the filters is 5 microns and they can be changed as much as 14 times per day although in average they are change 4 to 6 times.
The minimum flow control is kept by an ARC valve sized to allow the 70 gpm of minimum flow to recycle back to the column. I noticed though the Operators keep this valve closed on both pumps, I asked why (nobody seemed to know) until a Supervisor told me they decided to do that because the pump trips on overload when they keep it open. This did not make to much sense to me then (overload on min. flow condition?….keep reading).
Tests performed in the field
The conventional pressure gauge, amps reading, temps, vibration were done, herein the results:
First Test:
Pump “A”
Suction Press. = 22.5 PSIG
Disch. Press = 137 PSIG
Pump Casing Temp. = 232 *F (Max.)
Amps. = 17,7 (average)
Column Level = 40%
Pump “B’ (after shuting down “A”, “B” was coming from Maintenance – New Pump).
Suction Press. = 22.5 PSIG
Disch. Press = 134 PSIG
Pump Casing Temp. = 223 *F (Max.)
Amps. = 17 (average)
Column Level = 40%
A few minutes later the feed to the tower (waste water) was increased from 88 gpm to 176 gpm, the suction pressure increased to 25 psig and the discharge dropped to 131 psig. The amps drawn by the motor at that time was 22.2 (average). Aproximately 1 hour later the feed was cut back to 88 gpm and the pump was kept running. Ops were happy….
Six hours later Ops switched to pump “A” as pump “B” (new pump) was not capable of keeping up the column level. As normally occurs this happened late at night when there was nobody around to troubleshoot, process data does not show much either.
Second Test (the following day – I didn’t give up…), asked them to switch pumps, the results:
Pump “B”
Suction Press. = 24 PSIG
Disch. Press = 136 PSIG
Amps. = 18,4 (average)
Column Level = 38%
Pump was kept running with no issues, Ops happy again but not quite convinced (neither I was). At this time was when I noticed the ARC valve isolated, I explained the Operator the importance of keeping this valve lined up and kindly asked to open it although he refuses because “always have been isolated” although he didn’t know why, I told him I would find out, didn’t give up……
Returned a few hours later and after obtaining the approval of the Plant Supervisor we decided to open the ARC valve in order to "keep the pump protected". The conditions on the pump before opening this valve were:
Suction Press. = 23 PSIG
Disch. Press = 136 PSIG
Amps. = 18,7 (average)
Let's what happened a few seconds after the operator started opening this valve? wala! discharge pressure dropped and surged badly, the whole system started shaking, pump vibrated, became noisy and obviously the level on the column increased considerably (besides I became not very popular in the control room). The operator quickly switched to pump “A” which also showed the before describe symptoms, the operator cracked opened a vent in the pump casing and the pump recovered slowly (this trick didn’t worked in pump “B” though).
I gave up keep doing tests…..until having something.
Additional info:
For some reason Operators seem to have preference for pump “A” over pump “B”, even when having “new” pump "B" (like in this case) the pump does not perform as well as pump “A” (which is not good either). In terms of piping configuration pump “B” is a bit different as you can see in the attached sketch of the ISO.
Sorry for the lengthy of this post but I wanted to bring as much information as possible, maybe I’m over analyzing the problem (Do you guys golf?, have you heard the term “paralysis by analysis” when facing an important shot?.). I know there are some deviations in the system (the filtration unit downstream, the suspicious material of the casing, the ARC valve being closed, etc.) still this does not explains the symptoms and some of the damages.
My thoughts:
1.- Operating off the BEP and moving back and forth on the curve when changing filters creates radial loads that progressively worn out the radial bearing and then a snowball effect comes: wear rings worn, internal recirc., unbalance, vibration, seal fails, etc….
2.- Particles in the fluid eroded-corroded the casing which is probably of a different material despite of what the data sheet says (I’ve requested a PMI but the casing may have been scrapped already).
3.- Why would the pump cavitate (or water hammered?) when the arc valve was opened. At the beginning I said to myself of course! we went to the very right of the curve and made it cavitate but hold on…....no flow was supposed to pass through this valve as we were not in a low flow condition! or it was?.
4.- I doubt of real cavitation as I could not see the typical signs on the impeller (yes I used a mirror and looked closely every single section of the vanes), just saying, I'm not an expert in cavitation.
5.- As of today I have seen the damages just in one of the pumps ("B" pump), I can't say for sure the damages are the same to the other pump.
Sorry I made you read all this but I wanted complains they were not enough info (pretty sure someone will ask for more details though…...working on it).
Please do not forget look at the attachment and kindly contribute to this diagnose.
Thanks!
PS: I apologize if my grammar is not that perfect….yo hablo espanol).
Regards
Looking for some advice here.
I'm new to this plant and have been assigned to solve a recurrent problem on a couple of pumps which MTBF is around 3 months combined, the characteristics and operating conditions as follows:
Pump Type; API OH4 (not very fan of these particular type of pumps by the way)
Rated Flow: 260 gpm
Normal Flow (Data Sheet): 237 gpm
Actual Flow: It varies from 154 to 176 gpm ( 56 to 64 of the BEP)
BEP: 275 gpm
Diff. Head: 237 ft
Fluid Temp.: 264 *F
Fluid: Waste Water (Traces of CO2, NH3, HCN, particles / soot fines)
S.G: 0.936
Nss: 9660
Ns:487
Speed: 3600 rpm
Impeller Diam. = 8.5”
NPSHa (Data Sheet): 13 ft
NPSHa (Calculated - Suction Gauge Pressure Method): 12 ft
Min. Flow: 70 gpm
Suction Pipe: 4.5 times straight run of pipe diameters.
Inlet Velocity: < 3.5 FPS
Volute Type: Single
Materials: A351 CF3M (Impeller, Casing Cover, Volute), Ni-Resist (Wear rings)
Mechanical Seal: JC 2800 / API Plan 74 + 13 (1 1/8"shaft diam.).
Symptoms / Findings:
I’ve been quite a bit in the field checking these pumps and a “mild” cavitation like noise could be heard all the times although may becomes worse and make all the system to shake badly (similar to water hammer), this have caused in the past cracks on weldings, supports to come loose, failed bolts, etc., slight pressure fluctuations at the discharge are evident too. I have seen this happening even when a new (spare) pump installed.
Vibration could be severe at times but in my opinion this is a consequence after the radial sleeve bearing (carbon) gets worn and the wear ring rubs and get unbalanced, high speed and a massive rigid coupling make things worse.
I have had the opportunity to inspect these pumps internally a couple of times after they failed, I will let the pictures to speak for themselves. One thing that caught my attention though was the condition of the casing compared to the impeller being made of the same materials (although I’m pretty sure they are not) which tells me sometime on the run they may have been changed (I’m tracking this with the OEM). This does not explain the problem I’m describing though, does it?. Erosion-corrosion, recirculation cavitation?.
Control / Operating / Process conditions:
The system operates on level control, waste water and high particle filtrate is fed to the tower while live steam 50 PSI is injected in the mid section of the column, normal level is 50% although most of the times is at 40%. Control of particle content seems to be an issue upstream (still working with Process eng. to understand the problem). Flow meter and one of the level controllers is not working either (working with E/I to see if it’s a process related failure) so basically the control is manual. Pump was originally provided with basket strainers at the suction but they were removed most likely because of previous failures were attributed to cavitation, a filtration system was installed downstream of the pumps instead. This filtration system operates with a battery of 3 filters in parallel and three other filters in standby, the control is completely manual, a crew of operators monitor the dP across the filters and switch to the standby filters (which is kept pressurized) when the differential pressure reach the alarm values. The mesh of the filters is 5 microns and they can be changed as much as 14 times per day although in average they are change 4 to 6 times.
The minimum flow control is kept by an ARC valve sized to allow the 70 gpm of minimum flow to recycle back to the column. I noticed though the Operators keep this valve closed on both pumps, I asked why (nobody seemed to know) until a Supervisor told me they decided to do that because the pump trips on overload when they keep it open. This did not make to much sense to me then (overload on min. flow condition?….keep reading).
Tests performed in the field
The conventional pressure gauge, amps reading, temps, vibration were done, herein the results:
First Test:
Pump “A”
Suction Press. = 22.5 PSIG
Disch. Press = 137 PSIG
Pump Casing Temp. = 232 *F (Max.)
Amps. = 17,7 (average)
Column Level = 40%
Pump “B’ (after shuting down “A”, “B” was coming from Maintenance – New Pump).
Suction Press. = 22.5 PSIG
Disch. Press = 134 PSIG
Pump Casing Temp. = 223 *F (Max.)
Amps. = 17 (average)
Column Level = 40%
A few minutes later the feed to the tower (waste water) was increased from 88 gpm to 176 gpm, the suction pressure increased to 25 psig and the discharge dropped to 131 psig. The amps drawn by the motor at that time was 22.2 (average). Aproximately 1 hour later the feed was cut back to 88 gpm and the pump was kept running. Ops were happy….
Six hours later Ops switched to pump “A” as pump “B” (new pump) was not capable of keeping up the column level. As normally occurs this happened late at night when there was nobody around to troubleshoot, process data does not show much either.
Second Test (the following day – I didn’t give up…), asked them to switch pumps, the results:
Pump “B”
Suction Press. = 24 PSIG
Disch. Press = 136 PSIG
Amps. = 18,4 (average)
Column Level = 38%
Pump was kept running with no issues, Ops happy again but not quite convinced (neither I was). At this time was when I noticed the ARC valve isolated, I explained the Operator the importance of keeping this valve lined up and kindly asked to open it although he refuses because “always have been isolated” although he didn’t know why, I told him I would find out, didn’t give up……
Returned a few hours later and after obtaining the approval of the Plant Supervisor we decided to open the ARC valve in order to "keep the pump protected". The conditions on the pump before opening this valve were:
Suction Press. = 23 PSIG
Disch. Press = 136 PSIG
Amps. = 18,7 (average)
Let's what happened a few seconds after the operator started opening this valve? wala! discharge pressure dropped and surged badly, the whole system started shaking, pump vibrated, became noisy and obviously the level on the column increased considerably (besides I became not very popular in the control room). The operator quickly switched to pump “A” which also showed the before describe symptoms, the operator cracked opened a vent in the pump casing and the pump recovered slowly (this trick didn’t worked in pump “B” though).
I gave up keep doing tests…..until having something.
Additional info:
For some reason Operators seem to have preference for pump “A” over pump “B”, even when having “new” pump "B" (like in this case) the pump does not perform as well as pump “A” (which is not good either). In terms of piping configuration pump “B” is a bit different as you can see in the attached sketch of the ISO.
Sorry for the lengthy of this post but I wanted to bring as much information as possible, maybe I’m over analyzing the problem (Do you guys golf?, have you heard the term “paralysis by analysis” when facing an important shot?.). I know there are some deviations in the system (the filtration unit downstream, the suspicious material of the casing, the ARC valve being closed, etc.) still this does not explains the symptoms and some of the damages.
My thoughts:
1.- Operating off the BEP and moving back and forth on the curve when changing filters creates radial loads that progressively worn out the radial bearing and then a snowball effect comes: wear rings worn, internal recirc., unbalance, vibration, seal fails, etc….
2.- Particles in the fluid eroded-corroded the casing which is probably of a different material despite of what the data sheet says (I’ve requested a PMI but the casing may have been scrapped already).
3.- Why would the pump cavitate (or water hammered?) when the arc valve was opened. At the beginning I said to myself of course! we went to the very right of the curve and made it cavitate but hold on…....no flow was supposed to pass through this valve as we were not in a low flow condition! or it was?.
4.- I doubt of real cavitation as I could not see the typical signs on the impeller (yes I used a mirror and looked closely every single section of the vanes), just saying, I'm not an expert in cavitation.
5.- As of today I have seen the damages just in one of the pumps ("B" pump), I can't say for sure the damages are the same to the other pump.
Sorry I made you read all this but I wanted complains they were not enough info (pretty sure someone will ask for more details though…...working on it).
Please do not forget look at the attachment and kindly contribute to this diagnose.
Thanks!
PS: I apologize if my grammar is not that perfect….yo hablo espanol).
Regards