Milutin
Chemical
- Jul 7, 2006
- 152
Hi all,
Is it possible describe clear symptoms for following reformer problems:
- metal poisoning
- overchlorinated catalyst
- underchlorinated catalyst
- catalyst end of life
- problems caused by poor regeneration
Our reformer has following deviations from normal operations:
- low dT on first two reactors
- low H2 content in recycle gas (below 50%)
- low H2 production
- low reformate production, 10% lower than expected
- slightly higher then expected LEP factor (C1+C2)/(C3+C4)
- RON below 90(after last start up)
- and after last start up no response of naphta RON after reactor temperature increase
Catalyst is regenerated and 10 days after start up we had emergency shutdown, after start up we have slight but continuous loss of reforming performance.
After that we had three more shoot downs and faster loss of performance after every start up. All shoot downs are performed according user manual. Cycle length is five months and this is seventh cycle.
Chloride and water content in recycle gas are within expected values. Sulfur level in hydrotreated naphtha is 0.5ppm. Inlet reactor temperatures are 500degC.
What can cause such behavior?
Is it possible describe clear symptoms for following reformer problems:
- metal poisoning
- overchlorinated catalyst
- underchlorinated catalyst
- catalyst end of life
- problems caused by poor regeneration
Our reformer has following deviations from normal operations:
- low dT on first two reactors
- low H2 content in recycle gas (below 50%)
- low H2 production
- low reformate production, 10% lower than expected
- slightly higher then expected LEP factor (C1+C2)/(C3+C4)
- RON below 90(after last start up)
- and after last start up no response of naphta RON after reactor temperature increase
Catalyst is regenerated and 10 days after start up we had emergency shutdown, after start up we have slight but continuous loss of reforming performance.
After that we had three more shoot downs and faster loss of performance after every start up. All shoot downs are performed according user manual. Cycle length is five months and this is seventh cycle.
Chloride and water content in recycle gas are within expected values. Sulfur level in hydrotreated naphtha is 0.5ppm. Inlet reactor temperatures are 500degC.
What can cause such behavior?