npower0073
Electrical
- Jun 24, 2007
- 70
On site we have a three winding step up transformer 440MVA, 400kV/15.75kV/15kV. Lately we made maintenacne on the tap changer (MR), changed the oil and put back in service. After 10 days we made ne oil analysis and after 40 days we made a second oil analysis. The results of the first analysis were OK, the results of the second showed onyl increased gas ppm (more than 100 ppm) and showed that very good oil dielectric strength. We suspect that there is arching inside the tap cahgner contacts. Can you please give some feed back on that issue? Next week we will make the third consequitive sampling.