RandySavage
Mechanical
- Jul 15, 2021
- 6
Hello All,
Trying to qualify a procedure for welding 9% Chrome material (Grade 91) to itself with ERNiCr-3 N06082 filler metal - in accordance with the parameters laid out in the NBIC Section 3 book's Weld Method 6.
For any interested it can be found in section 2.5.3, 2.5.3.6.
This weld method gives guidelines that must be followed and various restrictions to variables in order to not PWHT the P91 material. I know that 9% Cr is somewhat taboo to bring up, but the reality is that it exists and people continue to struggle with it. Please note this is not for new builds and only pertains to repairs of Grade 91 boiler tube specifically, internal to the boiler, with a maximum size of NPS 5 in diameter and 1/2" MWT for which notch toughness testing was not required. Our normal procedures surrounding 9% Cr do use appropriate filler metal with PWHT, but just trying to stay on-top of certain things in the industry changing.
I was wondering if anyone else has tried coming up with a process for this, and if so if there were any tips or advice that could be offered.
The problem I'm currently facing is that when bending the roots there is some form of failure in the weld joint itself, from the first attempt of snapping it in half to more recent attempts with changing some of our methods that are still failing but at least not to the same degree. The only consistency is that the caps are bending quite well. Unsure if it is the heat cycling, heat distribution due to rig angle changing, etc.
All of this is being done entirely with the GTAW process.
Base material is SA 335 P91 Type 1, 2-1/2" Sch 80(0.276")
Filler Metal is ERNiCr-3, have 3/32" and 1/8"
Butt-welded, 3/32" Gap with 37.5 degree bevel is about average so far, trying both Argon purge and Solar Flux Type I.
Sorry for the length of this, but I figured some documentation of the process and changes we made may not only help determine errors here, but could be useful for others in the future.
1.) Started around 110 Amps with a preheat of 200 degrees F and never neared the interpass temp of 550 deg F. Tried Paste here, figured results may have been running too cold to burn out flux and that some may have been trapped. - Very bad results, but it was the initial trial.
2.) 110 Amp root again, but with 100% Argon purge. Slightly elevated preheat to 275 Deg F - hit 375 degrees F at completion of root. Hot pass hit 383 degrees, cap hit 430 degrees. Same results as first where root failed entirely, cap had some minor discontinuities but not terrible.
3.) Elevated Preheat to 300 degrees F - Wrapped with K-Wol in-between passes to reduce cooling rate. Rooted at 150 Amps with 3/32" wire, fill and cap done at 170 Amps with 3/32" as well. On cap we started to get close to the interpass temp reaching 515 Degrees. Root bend failed, but finally did not come apart, caps finally began to bend well and had no visible defects, but evidence of the HAZ of the base metal being strong and ductile is there. On these bends the failure was at the weld interface itself and not directly in the center of the weld. Seemed as though it wasn't strong enough to fully keep itself fused to the base metal.
4.) Preheat elevated to 400 Degrees, 1/8" gap however with a slight land this time of the bevels - near 1/32", 1/8" filler, 190 Amps for the root. Also wrapped to reduce cooling rate. Maximum temperature achieved was 515 Degrees. Cap again came out well, if anything the roots were worse than trial #3.
If you would like any additional info please just ask. We are continuing to try different methods, but if anyone has some additional tips or insight that would be much appreciated.
Thank you,
Trying to qualify a procedure for welding 9% Chrome material (Grade 91) to itself with ERNiCr-3 N06082 filler metal - in accordance with the parameters laid out in the NBIC Section 3 book's Weld Method 6.
For any interested it can be found in section 2.5.3, 2.5.3.6.
This weld method gives guidelines that must be followed and various restrictions to variables in order to not PWHT the P91 material. I know that 9% Cr is somewhat taboo to bring up, but the reality is that it exists and people continue to struggle with it. Please note this is not for new builds and only pertains to repairs of Grade 91 boiler tube specifically, internal to the boiler, with a maximum size of NPS 5 in diameter and 1/2" MWT for which notch toughness testing was not required. Our normal procedures surrounding 9% Cr do use appropriate filler metal with PWHT, but just trying to stay on-top of certain things in the industry changing.
I was wondering if anyone else has tried coming up with a process for this, and if so if there were any tips or advice that could be offered.
The problem I'm currently facing is that when bending the roots there is some form of failure in the weld joint itself, from the first attempt of snapping it in half to more recent attempts with changing some of our methods that are still failing but at least not to the same degree. The only consistency is that the caps are bending quite well. Unsure if it is the heat cycling, heat distribution due to rig angle changing, etc.
All of this is being done entirely with the GTAW process.
Base material is SA 335 P91 Type 1, 2-1/2" Sch 80(0.276")
Filler Metal is ERNiCr-3, have 3/32" and 1/8"
Butt-welded, 3/32" Gap with 37.5 degree bevel is about average so far, trying both Argon purge and Solar Flux Type I.
Sorry for the length of this, but I figured some documentation of the process and changes we made may not only help determine errors here, but could be useful for others in the future.
1.) Started around 110 Amps with a preheat of 200 degrees F and never neared the interpass temp of 550 deg F. Tried Paste here, figured results may have been running too cold to burn out flux and that some may have been trapped. - Very bad results, but it was the initial trial.
2.) 110 Amp root again, but with 100% Argon purge. Slightly elevated preheat to 275 Deg F - hit 375 degrees F at completion of root. Hot pass hit 383 degrees, cap hit 430 degrees. Same results as first where root failed entirely, cap had some minor discontinuities but not terrible.
3.) Elevated Preheat to 300 degrees F - Wrapped with K-Wol in-between passes to reduce cooling rate. Rooted at 150 Amps with 3/32" wire, fill and cap done at 170 Amps with 3/32" as well. On cap we started to get close to the interpass temp reaching 515 Degrees. Root bend failed, but finally did not come apart, caps finally began to bend well and had no visible defects, but evidence of the HAZ of the base metal being strong and ductile is there. On these bends the failure was at the weld interface itself and not directly in the center of the weld. Seemed as though it wasn't strong enough to fully keep itself fused to the base metal.
4.) Preheat elevated to 400 Degrees, 1/8" gap however with a slight land this time of the bevels - near 1/32", 1/8" filler, 190 Amps for the root. Also wrapped to reduce cooling rate. Maximum temperature achieved was 515 Degrees. Cap again came out well, if anything the roots were worse than trial #3.
If you would like any additional info please just ask. We are continuing to try different methods, but if anyone has some additional tips or insight that would be much appreciated.
Thank you,