retired13 said:
Don't sound the alarm. Also 1.04626mm max. deflection? Can you provide beam size and length?
This is linear (eigenvalue) buckling analysis. I'm only putting a nominal 1kNm on each end and then running the model to reach the buckling modes. The displacement is meaningless. (I could probably do a non linear buckling analysis with the result of the linear analysis but this is a fair bit of work.)
retired13 said:
Note, Yuri and AISC requires one of the two types of restraint, torsion or translation, to be considered effective.
Well yeah. That was my point. The joints don't provide transnational bracing. I've now stated many times that they do offer some torsional restraint. However like I have said torsional bracing if it isn't stiff enough isn't going to reduce the effective length to the joist spacing. I have seen little good guidance on the effect of torsional stiffness of members and connections and it's effect in reducing the effective length. My local code seems to ignore it completely (AS4100). This is where more complex buckling analysis comes in. The effective length concept is really just a simplifying shortcut.
retired13 said:
Yes, the OP didn't mention flooring, but just by engineering judgement, what is that support system is likely for?
Not all flooring can be relied upon as an effective diaphragm. Again this was discussed at the end of the previous thread.
EDIT
OK I ran the non linear analysis of the same beam displayed earlier. (2 pins in restraint, buckled 41.75kN) I put 50kN into it in 5kN increments.
25kN: 23.5mm max deflection (0.94mm/kNm)
30kN: 28.3mm max deflection (0.94mm/kNm)
35kN: 33.1mm max deflection (0.94mm/kNm)
40kN: 38.4mm max deflection (0.96mm/kNm) twisting barely perceptible
45kN: 44.6mm max deflection (0.99mm/kNm) slight twisting
50kN: 70.3mm max deflection (1.41mm/kNm) significant buckling twist
As you can at 40kN and 45kN the max deflection has increased slightly indicating that it is starting to buckle. At 50kN the beam has well and truly buckled
(Deflection NOT to scale)
Note this too 15mins just to process the analysis, most of that time was spent on convergence on the last increment. That is why non linear buckling analysis is alot of work!