NTSB Meeting Miami 1:19 into recording re Cold Joints.
Vice Chair asked about a % difference ( loss) in AASHTO preparation and the joints as constructed. Well, not that clearly asked, but that was the gist of the query.
Staff could not respond off the cuff - and missed a perfect opportunity to go into the difference in coefficient of friction and factor of 1.0 vs 0.6, which clearly is a 40% loss of capacity.
The discussion did not cover the fact that FIGG design was based on AASHTO "roughened to 1/4" amplitude" but instructions to the job were to follow FDOT specification, which is quite different. They did discuss whether the drawings required AASHTO 1/4" and the fact that the details did not show that requirement.
I would like to have seen a discussion that covered the fact that if the design were based on no intentional roughening of the joints, the joints would then require more steel reinforcing across the joint and could be made adequate to resist the demand.
I got the feeling the discussion was slanted to the benefit of MCM.
I have wondered if FDOT intentionally left off the requirement for the 1/4" amplitude, and in doing so are requiring a design with more steel reinforcing across the shear plane. I think that could provide a more predictable capacity.
Does FDOT accept the AASHTO 1/4" prepped joint with a mu of 1.0? Is the FDOT spec joint prep assigned a mu of 0.6?
I have assumed the FDOT spec was to provide weather resistant joints which would bleed less and be more durable.
Interesting that Bolton Perez basically recommended special attention to the joints but did not push a recommendation in that regard. Then FIGG back tracked from their design basis by referencing FDOT. Apparently FTGG did not know the difference.
Then later in the meeting, NTSB presses the point that the structure would likely fail regardless of the joint preparation, because the design was so deficient. Again letting MCM off the hook.
I am going out on a limb here but with the joint as intended by FIGG it would have 66% more capacity and maybe not have failed when it did. Had it lasted 6 months and the back span been completed, this joint might not have been the critical point. But there were other issues, and this may have been the most fortunate time. That offers no comfort to the families of those lost and to those injured.